|
Gulf of
Mexico Region
Fires 1999
| Date: |
02-Jan-1999 |
Operator: |
Shell Offshore, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G11455 |
Event(s): |
Fire |
| Area: |
Garden Banks |
Operation: |
Production |
| Block: |
128 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A |
Water Depth: |
705 feet |
Remarks: A small fire occurred, resulting in
minor damage to pipeline pump PAX-6040B. The seals failed, allowing excessive temperature
to build up due to friction; this ignited the remaining lubricating oil. The seal and pump
manufacturers performed a root cause analysis.
| Date: |
09-Jan-1999 |
Operator: |
Ocean Energy, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G04270 |
Event(s): |
Fire |
| Area: |
South Marsh Island |
Operation: |
Production |
| Block: |
243 |
Cause: |
Equipment Failure |
| Rig/Platform: |
C |
Water Depth: |
23 feet |
Remarks: A small fire occurred, involving one of two
platform generators. The #2 generator winding was found smoking with no visible flames.
The insulation (epoxy coating) started to smolder, which kept the heat in the winding and
allowed the copper to burn. A CO2 fire extinguisher was used to cool and
contain the smoldering generator winding. Damage was restricted to the generator.
| Date: |
15-Jan-1999 |
Operator: |
Shell Offshore, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
00445 |
Event(s): |
Fire |
| Area: |
Eugene Island |
Operation: |
Production |
| Block: |
176 |
Cause: |
Human Error |
| Rig/Platform: |
JC |
Water Depth: |
83 feet |
Remarks: A minor flash fire occurred. A welding
operation to repair a hand railing on the top deck was in progress at the same time as a
natural gas crane was in use. Slag sparks from the welding operation came into contact
with the gas being exhausted from the crane. The crane was shut down and the fire was
extinguished. No damage was reported.
| Date: |
16-Jan-1999 |
Operator: |
Chevron U.S.A., Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G00983 |
Event(s): |
Fire |
| Area: |
Eugene Island |
Operation: |
Production |
| Block: |
252 |
Cause: |
Human Error |
| Rig/Platform: |
I |
Water Depth: |
150 feet |
Remarks: A small fire occurred during the installation of a
new compressor panel. An offshore technician cut through an energized wire, and caused a
spark that ignited a small amount of oil. The oil had accumulated in the compressor skid
pan as he was disconnecting old wiring from the existing compressor panel. The fire was
immediately extinguished with rags. No damage was reported.
| Date: |
18-Jan-1999 |
Operator: |
Shell Offshore, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G01294 |
Event(s): |
Fire |
| Area: |
South Pass |
Operation: |
Production |
| Block: |
62 |
Cause: |
Human Error |
| Rig/Platform: |
B |
Water Depth: |
322 feet |
Remarks: A compressor backfired when it was restarted
without completely purging the cylinders of fuel gas. The resulting sparks or flame from
the backfire ignited gases coming from a nearby glycol still column vent. The fire was
quickly extinguished using a seawater hose. There was no significant damage to equipment.
| Date: |
23-Jan-1999 |
Operator: |
Vastar Resources, Inc. |
| Investigation: |
None |
Activity: |
Exploration |
| Lease: |
G15780 |
Event(s): |
Fire |
| Area: |
High Island |
Operation: |
Drilling |
| Block: |
A1 |
Cause: |
Human Error |
| Rig/Platform: |
Cliffs Drilling 154/Cais. #2 |
Water Depth: |
55 feet |
Remarks: A welder caused a small flash fire while starting
to cut the 18 5/8-inch surface casing after the cement job. The wellhead area and the 18
5/8-inch by 30-inch annulus were checked with a gas detector; there was no evidence of
gas. The annular fluid was 6 feet below the wellhead when the cut began. Slag fell into
the annulus and caused the flash fire. The annulus was then filled with water and bubbles
were observed migrating through the fluid. The annulus was squeezed from the surface to
ensure isolation prior to nippling down the diverter and further cutting of the casing.
There was no damage to equipment.
| Date: |
23-Jan-1999 |
Operator: |
Shell Frontier Oil & Gas,
Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G01294 |
Event(s): |
Fire |
| Area: |
South Pass |
Operation: |
Production |
| Block: |
62 |
Cause: |
Welding |
| Rig/Platform: |
A |
Water Depth: |
340 feet |
Remarks: While welding, a spark fell by the sump. A flash
fire occurred for approximately one second. The sump was covered by tarps.
| Date: |
23-Jan-1999 |
Operator: |
Shell Deepwater Production, Inc. |
| Investigation: |
None |
Activity: |
Exploration |
| Lease: |
G06896 |
Event(s): |
Fire |
| Area: |
Viosca Knoll |
Operation: |
Drilling |
| Block: |
956 |
Cause: |
Exhaust Spark |
| Rig/Platform: |
A (Ram-Powell)/H&P 202 |
Water Depth: |
3,214 feet |
Remarks: A fire occurred on the exhaust piping from an EMD
engine on the rig. An exhaust spark ignited some residual oil on the exhaust piping. The
emergency response alarm was initiated. The fire was extinguished with a 30-lb chemical
unit in less than two minutes. No damage was reported.
| Date: |
26-Jan-1999 |
Operator: |
Vastar Resources, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G01608 |
Event(s): |
Fire |
| Area: |
South Pass |
Operation: |
Production |
| Block: |
60 |
Cause: |
Human Error |
| Rig/Platform: |
C |
Water Depth: |
205 feet |
Remarks: While enlarging mounting holes on a demister
bundle with a cutting torch, some residual paraffin was ignited by the heated metal and
resulted in a flash fire. The fire was extinguished using a 30-lb ABC dry chemical unit.
No property damage occurred.
| Date: |
29-Jan-1999 |
Operator: |
Vastar Resources, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G02137 |
Event(s): |
Fire |
| Area: |
South Pass |
Operation: |
Production |
| Block: |
60 |
Cause: |
Human Error |
| Rig/Platform: |
B |
Water Depth: |
206 feet |
Remarks: A light fixture was opened to verify its operating
voltage; the bare wires inside ignited a fire. The fire was extinguished with handheld
equipment and the appropriate electrical circuits were turned off.
| Date: |
07-Feb-1999 |
Operator: |
Shell Offshore, Inc. |
| Investigation: |
Complete |
Activity: |
Development/Production |
| Lease: |
G13607 |
Event(s): |
Fire/Injury (1) |
| Area: |
South Marsh Island |
Operation: |
Production |
| Block: |
40 |
Cause: |
Equipment Failure/Human
Error/External Damage |
| Rig/Platform: |
JA |
Water Depth: |
97 feet |
Remarks: A platform operator working alone on the platform
sustained 2nd and 3rd degree burns to 26% of his body, two fractured ribs, and a separated
shoulder. He was in the living quarters when he heard something blow out and continue to
blow. He exited the quarters to determine the cause and observed liquid blowing from the
#121 condensate pump. He went to the pump and was reaching for the suction valve handle
when the escaping liquids/gases ignited. He sustained the immediate flash of the fire and
made his way to a stairwell, where he tripped and fell down the stairway approximately 15
feet. Manual activation of the boat landing ESD or automatic detection and activation of
the fusible fire loop system over the condensate pump skid resulted in total platform shut
down. The fire continued due to the uncontrolled release of hydrocarbons. A pilot flying
in the area reported the fire to a Shell facility nearby. The M/V Cecilia C rescued the
operator from the structure. The fire apparently started at the #121 condensate pump. The
#2 and #3 ceramic plungers/pistons were severely cracked. Condensate and gas under
approximately 500 psi released uncontrolled to the atmosphere due to an apparent failure
of the #1 ceramic plunger/piston in the condensate pump. The plunger/piston failure cause
is uncertain, but likely resulted from thermal or acoustic (e.g. liquid hammer) shock.
| Date: |
11-Feb-1999 |
Operator: |
PennzEnergy Exploration and
Producing |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G02112 |
Event(s): |
Fire |
| Area: |
Eugene Island |
Operation: |
Production |
| Block: |
315 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A |
Water Depth: |
240 feet |
Remarks: The platform diesel generator was started for
power. While offloading supplies from the work boat, an alarm sounded and the lights went
out. The operator noticed smoke coming from the cabinet of the skid mounted generator.
When he opened the door, flames were coming from each end of the generator armature. The
fire was put out with a dry chemical fire extinguisher.
| Date: |
15-Feb-1999 |
Operator: |
Newfield Exploration Company |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G01604 |
Event(s): |
Fire |
| Area: |
West Delta |
Operation: |
Production |
| Block: |
152 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A |
Water Depth: |
373 feet |
Remarks: A small fire occurred when a gas leak on a failed
flange gasket was ignited from an undetermined source. Vibration was the suspected cause
of the gasket failure because one of the bolts in the flange was missing. The flange was
located on a 2-inch line from the compressor starter exhaust line to the vent system. The
gas source was either a leaking valve upstream of the starter or gas migration from the
vent system.
| Date: |
04-Mar-1999 |
Operator: |
IP Petroleum Company, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G16435 |
Event(s): |
Fire |
| Area: |
South Timbalier |
Operation: |
Production |
| Block: |
211 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A |
Water Depth: |
150 feet |
Remarks: An operator saw smoke coming from a glycol
reboiler. He removed some metal shielding and saw an 8-inch by 8-inch fire, which he put
out with a 30-lb handheld chemical fire extinguisher.
| Date: |
10-Mar-1999 |
Operator: |
Shell Offshore, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G01294 |
Event(s): |
Fire |
| Area: |
South Pass |
Operation: |
Production |
| Block: |
62 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A |
Water Depth: |
340 feet |
Remarks: The generator winding failed, causing a build-up
of heat. The heat worked its way back to the starter panel in the MCC building, melting
the insulation on the wires; the exposed wires came into contact with electrical prints,
creating an over-heating situation. Personnel threw the smoldering items in a 5-gallon
bucket of water to extinguish the fire.
| Date: |
11-Mar-1999 |
Operator: |
Unocal Exploration Corporation |
| Investigation: |
None |
Activity: |
Exploration |
| Lease: |
G06157 |
Event(s): |
Fire |
| Area: |
High Island |
Operation: |
Drilling |
| Block: |
133 |
Cause: |
Equipment Failure |
| Rig/Platform: |
Cliff Drilling 200/Caisson A |
Water Depth: |
52 feet |
Remarks: A fire occurred on the drilling rigs #1
generator engine, a Detroit TIB 16-149 (approximately 1200 HP) engine. Bearings caused the
turbo charger to disintegrate. The automatic air intake shut down, immediately killing the
engine. The hot engine ignited the turbo-charger cooling oil. The fire re-ignited a couple
of times due to the previously heated engine. Nine 20-lb fire extinguishers and one dry
chemical extinguisher were used to put out the fire.
| Date: |
15-Mar-1999 |
Operator: |
Vastar Resources, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G11221 |
Event(s): |
Fire |
| Area: |
Mustang Island |
Operation: |
Production |
| Block: |
787 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A |
Water Depth: |
151 feet |
Remarks: The rod assembly and piston parted at the
crankshaft and exited the engine block on cylinders 4R and 4L, causing two small flames
about 2 inches high and 3/8-inch wide between the distance piece and the frame of the
compressor gasket area. Both flames were extinguished with a 30-lb dry chemical
extinguisher within 30-45 seconds. It is unknown at this time what caused the fire. There
was no damage to the compressor from the fire.
| Date: |
17-Mar-1999 |
Operator: |
Shell Offshore, Inc. |
| Investigation: |
Complete |
Activity: |
Development |
| Lease: |
G05889 |
Event(s): |
Fire |
| Area: |
Green Canyon |
Operation: |
Production |
| Block: |
65 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A (Bullwinkle) |
Water Depth: |
1,350 feet |
Remarks: A small electrical fire occurred when the oil
shipping pump and switchgear were being commissioned. The transformer failed
instantaneously as power was applied to bump the motor for the first time and the
autotransformer for the oil shipping pump shorted internally. The fire detection system
and electrical power disruption activated the platform's ESD system, although no
continuous flames were observed. Initial observation indicated that some smoke was
deposited on the surrounding switchgear. Two electrical engineers, the platform
electrician, and the I&E construction inspector examined the system and determined it
was safe to continue running the remainder of the 4,160-Volt equipment. This was the
second time this transformer has failed. The first failure was due to a logic fault in the
circuitry. The initial inspection revealed the second failure was due to an internal fault
in the insulation of the transformer; the manufacturers inspection of the failed
transformer confirmed these findings.
| Date: |
18-Mar-1999 |
Operator: |
Marathon Oil Company |
| Investigation: |
Complete |
Activity: |
Development/Production |
| Lease: |
G01874 |
Event(s): |
Fire/Explosion |
| Area: |
West Delta |
Operation: |
Production |
| Block: |
79 |
Cause: |
Equipment Failure/Human Error |
| Rig/Platform: |
B |
Water Depth: |
115 feet |
Remarks: An employee was alerted by an engine oil PSL alarm
on the gas lift compressor. The alarm initiated a compressor shut-in. The compressor
unloaded pressure as part of the shut-in procedure; the compressor engine slowed but
failed to shut down completely, so the employee went to get a mechanic. Upon returning, an
explosion occurred in the crankcase. Both men noticed a small fire in the exposed section
of the compressor crankcase and extinguished it immediately with a nearby water hose. The
compressor was shut down manually by closing the fuel valve.
| Date: |
18-Mar-1999 |
Operator: |
Pennzoil Exploration and
Producing |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
00420 |
Event(s): |
Fire |
| Area: |
Ship Shoal |
Operation: |
Production |
| Block: |
154 |
Cause: |
Equipment Failure |
| Rig/Platform: |
E |
Water Depth: |
60 feet |
Remarks: Welding slag from a construction project ignited a
small fire from a fitting on a small gas supply line. The fitting did not seal tightly.
The fire began sometime during the morning; however, it was not noticed until nightfall
due to the small intensity and height of the flame. The fire was quickly extinguished with
a 20-lb handheld dry chemical unit. No damage was reported.
| Date: |
21-Mar-1999 |
Operator: |
OXY U.S.A., Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G01673 |
Event(s): |
Fire |
| Area: |
Main Pass |
Operation: |
Production |
| Block: |
296 |
Cause: |
Equipment Failure |
| Rig/Platform: |
C |
Water Depth: |
220 feet |
Remarks: The fire alarm sounded and the platform shut-in.
When the platform operator exited the quarters building to investigate, he saw flames
approximately 3 feet high at the #1 gas compressor. He grabbed a handheld 30-lb Ansul fire
extinguisher and put out the fire on the second burst. Upon initial investigation, it
appeared that gas was leaking from a crack approximately 4 inches long in the third stage
discharge piping/pulsation bottle. The crack ran diagonally from the third stage discharge
piping (between the compressor cylinder and pulsation bottle), across a weld, and on to
the reinforcing pad of the pulsation bottle. This area was covered with insulation. No
signs of external corrosion were found.
| Date: |
21-Mar-1999 |
Operator: |
OXY U.S.A., Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G01673 |
Event(s): |
Fire |
| Area: |
Main Pass |
Operation: |
Production |
| Block: |
296 |
Cause: |
Equipment Failure |
| Rig/Platform: |
B |
Water Depth: |
225 feet |
Remarks: While making his rounds, the platform operator
noticed black smoke coming from the auxiliary generator enclosure. When he opened the
enclosure door to shut down the unit, he saw flames around the turbocharger. The operator
shut down the unit and put out the fire with a handheld 30-lb Ansul fire extinguisher.
Upon initial investigation, it appeared that the turbocharger had an internal failure,
causing high vibration. The high vibration stripped out the two bolts holding the oil
supply line to the turbocharger. The leaking oil ignited on the hot engine.
| Date: |
24-Mar-1999 |
Operator: |
Chevron U.S.A., Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G02177 |
Event(s): |
Fire |
| Area: |
South Pass |
Operation: |
Production |
| Block: |
49 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A |
Water Depth: |
300 feet |
Remarks: A turbine gas compressor oil lube line parted and
oil sprayed on the exhaust insulation, igniting a small fire. The TSE over the compressor
activated and shut down the compressor. The fire was put out immediately with fire pump
water and a 30-lb chemical extinguisher.
| Date: |
06-Apr-1999 |
Operator: |
PennzEnergy Company |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G02115 |
Event(s): |
Fire |
| Area: |
Eugene Island |
Operation: |
Production |
| Block: |
330 |
Cause: |
Equipment Failure |
| Rig/Platform: |
C |
Water Depth: |
254 feet |
Remarks: The platform operator observed a small generator
fire. The source of the fire was a small rubber hose that sprayed engine coolant between
the engine exhaust and insulation. The coolant residue apparently ignited after the water
flashed off due to the hot surface of the exhaust system. The small fire was immediately
extinguished with the use of a CO2 unit. The fire alarm was sounded and the
generator was shut down. There was no damage.
| Date: |
09-Apr-1999 |
Operator: |
Vastar Resources, Inc. |
| Investigation: |
Complete |
Activity: |
Development |
| Lease: |
G05359 |
Event(s): |
Fire/Explosion/Injury
(1)/Fatality (1)/Pollution |
| Area: |
East Cameron |
Operation: |
Production/Construction work |
| Block: |
60 |
Cause: |
Human Error |
| Rig/Platform: |
A |
Water Depth: |
50 feet |
Remarks: As part of deactivation of the platforms
process drain line system, a section of the high-pressure separators drain line was
being cut with an electrical bandsaw. Construction contract personnel stopped severing the
line because condensate flowed from the cut. After attempting to contain the spilled
condensate and observing no more liquids flowing from the cut, the workers continued to
cut the line. Condensate flowed from the cut and drenched the saw operator. The saw
ignited the condensate and the ensuing fire engulfed the worker, who died days later as a
result of the burns. Another worker was injured attempting to assist the burned worker.
The fire caused approximately one million dollars worth of damage to the platform and
approximately 15 gallons of condensate spilled into the Gulf. See OCS Report MMS
2000-029
for more details.
| Date: |
02-May-1999 |
Operator: |
Vastar Resources, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G01608 |
Event(s): |
Fire |
| Area: |
South Pass |
Operation: |
Production |
| Block: |
60 |
Cause: |
Equipment Failure |
| Rig/Platform: |
G |
Water Depth: |
56 feet |
Remarks: The heater plug connector on the fire pump
corroded and fell into the drip pan. The electrician went to check the fire pump failure;
he picked up the connector, and it arced and ignited an oily residue in the skid pan. The
fire was put out immediately with a 30-lb handheld extinguisher.
| Date: |
06-May-1999 |
Operator: |
Chevron U.S.A., Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G01294 |
Event(s): |
Fire |
| Area: |
South Pass |
Operation: |
Production |
| Block: |
62 |
Cause: |
Welding |
| Rig/Platform: |
A |
Water Depth: |
340 feet |
Remarks: Welding slag ignited oil accumulation in the skid
of a lact unit. Welding was approximately 25 feet from the skid. Oil accumulated in the
skid from a dripping ½-inch ball valve that was bumped open. The fire was extinguished
immediately with a 30-lb dry chemical unit.
| Date: |
07-May-1999 |
Operator: |
Conoco, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G04518 |
Event(s): |
Fire |
| Area: |
Green Canyon |
Operation: |
Production |
| Block: |
184 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A (Jolliet) |
Water Depth: |
1,760 feet |
Remarks: A small fire occurred in the insulation of the
compressor. The only real damage was to the insulation blanket. The fire was extinguished
with a 30-lb handheld dry chemical unit.
| Date: |
07-May-1999 |
Operator: |
Chevron U.S.A., Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G01294 |
Event(s): |
Fire |
| Area: |
South Pass |
Operation: |
Production |
| Block: |
62 |
Cause: |
Welding |
| Rig/Platform: |
A |
Water Depth: |
340 feet |
Remarks: Welding slag ignited an accumulation of oil in the
lact skid. Welding was taking place 25 feet from the skid. Oil was dripping in the skid
when a ½-inch ball valve was bumped open. The fire was extinguished immediately with a
30-lb dry chemical unit. This is a repeat of a similar incident the day before.
| Date: |
08-May-1999 |
Operator: |
Taylor Energy Company |
| Investigation: |
Complete |
Activity: |
Development/Production |
| Lease: |
G01187 |
Event(s): |
Fire |
| Area: |
South Marsh Island |
Operation: |
Production |
| Block: |
27 |
Cause: |
Human Error |
| Rig/Platform: |
A |
Water Depth: |
100 feet |
Remarks: A welder was cutting on a spool for a new Wemco
unit. It was believed that some slag fell between the boards and continued to smolder. The
boards had been watered down both before and after the welding job was completed.
| Date: |
17-May-1999 |
Operator: |
Exxon Corporation |
| Investigation: |
None |
Activity: |
Exploration |
| Lease: |
G01619 |
Event(s): |
Fire |
| Area: |
South Pass |
Operation: |
Drilling |
| Block: |
93 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A |
Water Depth: |
450 feet |
Remarks: A breaker for mud pump #2 ignited in MCC room. A
30-lb handheld unit was used to immediately extinguish the fire.
| Date: |
18-May-1999 |
Operator: |
Vastar Resources, Inc. |
| Investigation: |
Complete |
Activity: |
Development/Production |
| Lease: |
G04453 |
Event(s): |
Fire |
| Area: |
Eugene Island |
Operation: |
Production |
| Block: |
240 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A |
Water Depth: |
139 feet |
Remarks: A fire occurred on the exhaust of the fire pump #2
engine; it was extinguished immediately. A contractor technician and the platform operator
were performing the weekly route fire pump inspection. They were conducting a nozzle flow
test on a reel hose on the breezeway below the heliport. The fire pump was running at full
throttle (1000 - 1100 rpm), maintaining an engine oil pressure of 80 psi. A contractor
operator was monitoring the water pressure at the pump's discharge. The fire pump had been
running approximately 15 minutes when a ¼-inch oil line ruptured, spraying oil onto the
engine's hot manifold and turbo charger causing the fire. The contractor instantly shut
down the fire pump by pulling the manual shutdown switch and extinguished the fire with a
30-lb dry chemical handheld unit. Several pieces of electrical equipment and rubber hoses
were damaged.
| Date: |
29-May-1999 |
Operator: |
Shell Offshore, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G04240 |
Event(s): |
Fire |
| Area: |
South Timbalier |
Operation: |
Production |
| Block: |
300 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A |
Water Depth: |
337 feet |
Remarks: An operator found a pipeline pump electric motor
on fire while responding to an alarm. He shut off the power to the motor and used fire
water to put out the fire in 5 minutes. There was only damage to the motor and the pipe.
| Date: |
03-Jun-1999 |
Operator: |
Exxon Corporation |
| Investigation: |
None |
Activity: |
Exploration |
| Lease: |
00026 |
Event(s): |
Fire |
| Area: |
West Delta |
Operation: |
Drilling |
| Block: |
30 |
Cause: |
Human Error |
| Rig/Platform: |
Ensco 99 |
Water Depth: |
50 feet |
Remarks: An operator representative was cutting a rig
diesel line when a very small flame was detected. The fire was extinguished with a 30-lb
dry chemical unit. No damage was reported.
| Date: |
10-Jun-1999 |
Operator: |
Kerr-McGee Corporation |
| Investigation: |
None |
Activity: |
Exploration |
| Lease: |
G13065 |
Event(s): |
Fire |
| Area: |
Viosca Knoll |
Operation: |
Drilling |
| Block: |
869 |
Cause: |
Equipment Failure |
| Rig/Platform: |
Diamond Ocean Lexington |
Water Depth: |
1,718 feet |
Remarks: An electrical wire grounded out inside a
transformer, causing the wires to overheat and ignite inside the mud logging unit. A 30-lb
dry chemical fire extinguisher was used to put out the fire.
| Date: |
05-Jul-1999 |
Operator: |
Vastar Resources, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G01106 |
Event(s): |
Fire |
| Area: |
West Delta |
Operation: |
Production |
| Block: |
133 |
Cause: |
Equipment Failure/Human Error |
| Rig/Platform: |
B |
Water Depth: |
285 feet |
Remarks: Natural gas escaped from the #1 generator fuel gas
SDV. Due to faulty packing, the gas escaped through a weep hole. The ignition source was
welding and cutting from overhead of the SDV. The fire was extinguished immediately. The
SDV was not shielded by fire preventive tarp.
| Date: |
06-Jul-1999 |
Operator: |
Vastar Resources, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G05475 |
Event(s): |
Fire |
| Area: |
South Marsh Island |
Operation: |
Production |
| Block: |
205 |
Cause: |
Weather Related |
| Rig/Platform: |
A |
Water Depth: |
457 feet |
Remarks: The platform communication system was disabled and
damaged during a severe thunderstorm. A small flame on a communication motherboard was
detected by the platform operator and extinguished with a handheld CO2 unit.
Inspection revealed a 2-inch charred spot on the motherboard. No other damage to equipment
was reported.
| Date: |
09-Jul-1999 |
Operator: |
Texaco Exploration and Production |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G02118 |
Event(s): |
Fire |
| Area: |
Eugene Island |
Operation: |
Production |
| Block: |
338 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A |
Water Depth: |
253 feet |
Remarks: A small fire occurred when a clamp, located
between the expansion joint and the compressor engine exhaust, became dislocated allowing
a 2-foot flame to escape during a compressor start-up. The compressor was shut down and
allowed to cool so repairs could be performed. Insulation was removed from the area to
allow the clamp to be reinstalled. The flame immediately extinguished itself. There was no
damage to equipment.
| Date: |
11-Jul-1999 |
Operator: |
Exxon Corporation |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
00031 |
Event(s): |
Fire |
| Area: |
Grand Isle |
Operation: |
Production |
| Block: |
220 |
Cause: |
Equipment Failure |
| Rig/Platform: |
L-QTR |
Water Depth: |
55 feet |
Remarks: A rental 350-kW generator caught on fire due to
electrical motor winding. The fire was put out with a 30-lb handheld dry chemical unit.
The generator was returned to the contractor.
| Date: |
25-Jul-1999 |
Operator: |
EEX Corporation |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G07486 |
Event(s): |
Fire |
| Area: |
Garden Banks |
Operation: |
P&A Operation |
| Block: |
338 |
Cause: |
Human Error |
| Rig/Platform: |
A (Cooper) |
Water Depth: |
2,097 feet |
Remarks: A minor flash fire occurred while a welder was
repairing handrails near the moon pool. Fuel for the fire originated from a small
accumulation of oil or condensate inside the free standing production riser. The fire
extinguished itself immediately. There was no damage reported.
| Date: |
01-Aug-1999 |
Operator: |
Exxon Corporation |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G01619 |
Event(s): |
Fire |
| Area: |
South Pass |
Operation: |
Production |
| Block: |
93 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A |
Water Depth: |
450 feet |
Remarks: The #2 platform generator had a lubricating oil
line that leaked onto the exhaust manifold. The small fire extinguished itself within 15
seconds. The oil line was replaced.
| Date: |
03-Aug-1999 |
Operator: |
Vastar Resources, Inc. |
| Investigation: |
Complete |
Activity: |
Development/Production |
| Lease: |
G14585 |
Event(s): |
Fire |
| Area: |
Main Pass |
Operation: |
Drilling |
| Block: |
264 |
Cause: |
Equipment Failure |
| Rig/Platform: |
Ensco 51 |
Water Depth: |
224 feet |
Remarks: The Ensco rig electrician observed a fire on the
#1 main rig engine. The electrician shut off the fuel supply to the engine and sounded the
fire alarm. The derrickman extinguished the fire with a 30-lb carbon dioxide unit. There
was minimal damage to the engine and related equipment.
| Date: |
08-Aug-1999 |
Operator: |
Kerr-McGee Oil and Gas
Corporation |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G04832 |
Event(s): |
Fire |
| Area: |
Main Pass |
Operation: |
Air Conditioning Unit |
| Block: |
108 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A |
Water Depth: |
70 feet |
Remarks: A minor fire developed in an air conditioning unit
in the MCC room. The fire was extinguished and the air conditioning unit was replaced.
| Date: |
23-Aug-1999 |
Operator: |
Mobil Oil Corporation |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G02947 |
Event(s): |
Fire |
| Area: |
Main Pass |
Operation: |
Production |
| Block: |
73 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A |
Water Depth: |
110 feet |
Remarks: A small fire ignited on the KVSR gas compressor.
The fuel header gasket failed on the #11 cylinder and gas entered the coil box, which
ignited. The fire was extinguished immediately.
| Date: |
03-Sep-1999 |
Operator: |
Vastar Resources, Inc. |
| Investigation: |
Complete |
Activity: |
Development |
| Lease: |
G14528 |
Event(s): |
Fire |
| Area: |
South Timbalier |
Operation: |
Production |
| Block: |
145 |
Cause: |
Human Error |
| Rig/Platform: |
A |
Water Depth: |
94 feet |
Remarks: The operator filled the lube oil day tank for the
gas compressor and did not notice the fill valve to the generator lube oil day tank was
partially open. The lube oil was inadvertently pumped to the generator lube oil day tank
and over-filled, allowing the oil to pool on the roof of the generator building near the
generator exhaust pipe. The operator shut down the lube oil transfer pump upon filling the
compressor lube oil day tank and proceeded to the living quarters. The lube oil eventually
made contact with the generator engine exhaust insulation. The insulation guided the lube
oil down into the generator building and into contact with the exhaust pipe and engine;
the lube oil ignited in and around the generator exhaust pipe. The evolution of the fire
increased and the thermal plugs on both sides of the exhaust manifold melted. Initial
attempts to extinguish the flames inside the generator building were not successful. The
fire spread to the roof of the generator building where it melted a plastic tank filled
with flammable engine coolant, adding fuel to the fire. Personnel evacuated the platform
after all tries to extinguish the fire were exhausted.
| Date: |
08-Sep-1999 |
Operator: |
Exxon Corporation |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G03818 |
Event(s): |
Fire |
| Area: |
Mississippi Canyon |
Operation: |
Production |
| Block: |
280 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A (Lena) |
Water Depth: |
1,000 feet |
Remarks: A gas leak from tubing going to the dryer may have
made contact with the coil to ignite. This was on the #4 compressor. The fire was put out
with a 5-lb chemical extinguisher.
| Date: |
09-Sep-1999 |
Operator: |
Newfield Exploration Company |
| Investigation: |
Pending |
Activity: |
Development |
| Lease: |
G15412 |
Event(s): |
Blowout/Fire |
| Area: |
Ship Shoal |
Operation: |
Workover |
| Block: |
354 |
Cause: |
Pending |
| Rig/Platform: |
A |
Water Depth: |
463 feet |
Remarks: During a workover operation, coiled tubing parted
between the stripper assembly and the injector head allowing gas to escape to the
atmosphere. The crew shut the pipe rams, shear rams, and blind rams but the well still
flowed. The platform was shut in and all personnel were evacuated. On September 12, the
well caught on fire. This incident is under investigation by MMS.
| Date: |
10-Sep-1999 |
Operator: |
Burlington Resources Offshore,
Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
00806 |
Event(s): |
Fire |
| Area: |
Eugene Island |
Operation: |
Production |
| Block: |
206 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A |
Water Depth: |
100 feet |
Remarks: A small fire occurred on pipeline pump #1 when oil
from a bad oil tank carried over and splashed onto the pump exhaust piping. A high level
in the bad oil tank occurred because a malfunctioned BS&W monitor failed to alarm when
oil was inadvertently diverted to the bad oil tank. Carry over of the tank occurred due to
a LSH failure. The TSE and ESD activated and initiated platform shut-in. Platform
personnel extinguished the fire immediately.
| Date: |
13-Sep-1999 |
Operator: |
Marathon Oil Company |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G01449 |
Event(s): |
Fire |
| Area: |
West Delta |
Operation: |
Production |
| Block: |
79 |
Cause: |
Unknown |
| Rig/Platform: |
A |
Water Depth: |
112 feet |
Remarks: A small fire occurred in the air compressor on the
production deck. The ground wire for the air compressor broke and created static
electricity, causing a small internal fire. It was put out with a 30-lb dry chemical
extinguisher. Damage was limited to the air compressor.
| Date: |
13-Sep-1999 |
Operator: |
Chevron U.S.A., Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G05064 |
Event(s): |
Fire |
| Area: |
Mobile |
Operation: |
Crane |
| Block: |
864 |
Cause: |
Equipment Failure |
| Rig/Platform: |
B |
Water Depth: |
58 feet |
Remarks: There was an oil leak in an oil pressure tubing
line that vibrated against a 110-volt alternator on the crane engine. This resulted in a
small fire in the platform crane engine drip pan. It was extinguished immediately and
there was minimal damage.
| Date: |
14-Sep-1999 |
Operator: |
Shell Offshore, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G01220 |
Event(s): |
Fire |
| Area: |
Eugene Island |
Operation: |
Production |
| Block: |
158 |
Cause: |
Equipment Failure |
| Rig/Platform: |
C |
Water Depth: |
83 feet |
Remarks: A small electrical fire occurred due to a
centrifuge switch failure. The platform operator plugged in the electrical cord for the
unit, turned the machine on, and left the area. He returned five minutes later to discover
the switch had caught on fire. The fire was extinguished and the electrical cord was
unplugged.
| Date: |
16-Sep-1999 |
Operator: |
Conoco, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G04518 |
Event(s): |
Fire |
| Area: |
Green Canyon |
Operation: |
Production |
| Block: |
184 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A (Jolliet) |
Water Depth: |
1,700 feet |
Remarks: A platform operator opened a side door to a metal
enclosure/sound barrier. This let oxygen into the enclosure, and the oil-coated insulation
caught fire. The fire was quickly put out with a handheld extinguisher. The unit was then
shut down.
| Date: |
21-Sep-1999 |
Operator: |
Santa Fe Snyder Corporation |
| Investigation: |
Complete |
Activity: |
Development/Production |
| Lease: |
G07759 |
Event(s): |
Fire |
| Area: |
Ship Shoal |
Operation: |
Production |
| Block: |
299 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A |
Water Depth: |
258 feet |
Remarks: Compressor CBA 2020 experienced a shut-in, caused
by the engine stalling. The compressor went through its normal shutdown functions. At this
point, the SDV was closing while the BDV was opening. During the blowdown phase of the
shutdown, a 2-foot by 16-inch long stainless steel flex hose in the vent system on the
compressor skid failed. The failure of the hose caused gas that should have gone to the
flare scrubber to be vented locally. The lead operator responded to a production alarm
caused by the compressor shutdown. On the way to the production panel, he could see the
fire on the west side of the compressor skid near the engine; he activated the platform
ESD. The fire was put out in one minute with two 30-lb handheld dry chemical fire
extinguishers. The ignition source is undetermined.
| Date: |
22-Sep-1999 |
Operator: |
Marathon Oil Company |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G12136 |
Event(s): |
Fire |
| Area: |
Ewing Bank |
Operation: |
Production |
| Block: |
873 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A (Lobster) |
Water Depth: |
780 feet |
Remarks: Heat caused oil on bearings to catch fire. The
flame was about 8 inches high. One 30-lb handheld dry chemical fire extinguisher was used
to put out the fire. The location of the fire was the motor on the lact unit.
| Date: |
30-Sep-1999 |
Operator: |
Shell Deepwater Production, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G07963 |
Event(s): |
Fire |
| Area: |
Mississippi Canyon |
Operation: |
Production/Construction |
| Block: |
807 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A (Mars) |
Water Depth: |
2,930 feet |
Remarks: While filling the diesel tank on a rental air
compressor, the hose from the portable tank came loose and sprayed diesel on the exhaust
of the air compressor. The diesel ignited and was extinguished with a 20-lb dry chemical
unit. The fire lasted less than 30 seconds and damage was limited to wiring on the air
compressor.
| Date: |
04-Oct-1999 |
Operator: |
Shell Offshore, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G06896 |
Event(s): |
Fire |
| Area: |
Viosca Knoll |
Operation: |
Production |
| Block: |
956 |
Cause: |
Equipment Failure/Weather Related |
| Rig/Platform: |
A (Ram-Powell) |
Water Depth: |
3,216 feet |
Remarks: A portable fan caught on fire. The power to the
fan was cut off immediately and the fire was extinguished. The fan was located on a deck
outside the living quarters and was used to cool personnel on break. Weather and/or a
short circuit may have been a contributing cause.
| Date: |
09-Oct-1999 |
Operator: |
Chevron U.S.A., Inc. |
| Investigation: |
None |
Activity: |
Exploration |
| Lease: |
G05911 |
Event(s): |
Fire |
| Area: |
Green Canyon |
Operation: |
Drilling |
| Block: |
205 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A (Genesis)/Nabors 85 |
Water Depth: |
2,690 feet |
Remarks: A very small fire occurred when a natural gas fuel
line parted at a connection and leaked. Some nearby rags caught fire and were extinguished
with a handheld dry chemical fire unit. The actual fire was on the rig. The ignition
source is unknown.
| Date: |
13-Oct-1999 |
Operator: |
Exxon Corporation |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G03818 |
Event(s): |
Fire |
| Area: |
Mississippi Canyon |
Operation: |
Production |
| Block: |
280 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A (Lena) |
Water Depth: |
1,000 feet |
Remarks: On the booster sales compressor, the fuel line
leaked and came into contact with the coil, causing a small fire. The root cause appears
to be a bushing on the fuel line that was loosened due to vibration. The fire was
extinguished immediately with a 30-lb handheld chemical unit. "Lock-Tite" was
applied to all fittings.
| Date: |
18-Oct-1999 |
Operator: |
Vastar Resources, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G01106 |
Event(s): |
Fire |
| Area: |
West Delta |
Operation: |
Production |
| Block: |
133 |
Cause: |
Equipment Failure |
| Rig/Platform: |
B |
Water Depth: |
285 feet |
Remarks: On a platform generator, the piping between the
exhaust manifold and the expansion joint caught on fire. A leak of process oil from the
platform fuel gas system came into contact with the exhaust, causing the fire. It was
extinguished immediately.
| Date: |
22-Oct-1999 |
Operator: |
Chevron U.S.A., Inc. |
| Investigation: |
Pending |
Activity: |
Exploration |
| Lease: |
G16670 |
Event(s): |
Fire |
| Area: |
Mississippi Canyon |
Operation: |
Drilling |
| Block: |
1002 |
Cause: |
Pending |
| Rig/Platform: |
Falcon Deepwater Pathfinder |
Water Depth: |
6,950 feet |
Remarks: A failure occurred in the draw works while running
the BOP stack, the lower marine riser package (LMRP), and the riser assembly. The top
drive struck the rig floor and the BOP, LMRP, and riser assembly fell into the gulf. A
fire also occurred and was extinguished within a few minutes.
| Date: |
28-Oct-1999 |
Operator: |
Exxon Corporation |
| Investigation: |
Complete |
Activity: |
Development/Production |
| Lease: |
G03818 |
Event(s): |
Fire |
| Area: |
Mississippi Canyon |
Operation: |
Production |
| Block: |
280 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A (Lena) |
Water Depth: |
1,000 feet |
Remarks: The Pool 10 rig crew was performing routine
maintenance on rig components when a night driller noticed a flame in the compressor
building. The small fire was caused by an ignition coil on the #1 left bank head of the
booster compressor engine. He grabbed a 30-lb fire extinguisher and put out the fire. The
engine was shut down.
| Date: |
30-Oct-1999 |
Operator: |
Stone Energy Corporation |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G01152 |
Event(s): |
Fire |
| Area: |
Vermilion |
Operation: |
Production |
| Block: |
255 |
Cause: |
Human Error |
| Rig/Platform: |
A |
Water Depth: |
158 feet |
Remarks: After shutting in the wells, contract crews began
welding and cutting on the platform. While cutting on the heliport, slag fell through the
top deck grating and onto the panel board. Gas leaked out of regulators and ignited. The
only damage was to regulators inside the panel board.
| Date: |
01-Nov-1999 |
Operator: |
Exxon Corporation |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
00031 |
Event(s): |
Fire |
| Area: |
Green Canyon |
Operation: |
Production |
| Block: |
22 |
Cause: |
Equipment Failure |
| Rig/Platform: |
L-QTR |
Water Depth: |
55 feet |
Remarks: A small gas leak in the exhaust system on #6 gas
compressor ignited a small fire near the filter media and was extinguished immediately
with a 30-lb dry chemical unit. Damage was minimal.
| Date: |
02-Nov-1999 |
Operator: |
Union Pacific Resources Company |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G01520 |
Event(s): |
Fire |
| Area: |
Ship Shoal |
Operation: |
Production |
| Block: |
204 |
Cause: |
Human Error |
| Rig/Platform: |
B |
Water Depth: |
103 feet |
Remarks: Cutting and welding were taking place on the top
deck, Which was constructed of creosote boards. Two operators on Platform A noticed a deck
fire on the platform and notified the site supervisor of Platform B. The M/V Mr. Andre
fought the fire for a short time. A helicopter dropped two operators on the platform; the
fire was extinguished using six 30-lb handheld dry chemical units.
| Date: |
08-Nov-1999 |
Operator: |
Mobil Exploration and Producing |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G05057 |
Event(s): |
Fire |
| Area: |
Mobile |
Operation: |
Battery for fire water pump |
| Block: |
823 |
Cause: |
Human Error |
| Rig/Platform: |
A |
Water Depth: |
65 feet |
Remarks: The battery cable lead wire connection was loose.
A spark from the loose connection caught grease on fire and went out on its own.
| Date: |
09-Nov-1999 |
Operator: |
Union Oil Company of California |
| Investigation: |
None |
Activity: |
Exploration |
| Lease: |
G01228 |
Event(s): |
Fire |
| Area: |
Ship Shoal |
Operation: |
Drilling |
| Block: |
208 |
Cause: |
Unforeseeable Occurrence |
| Rig/Platform: |
H |
Water Depth: |
100 feet |
Remarks: While cutting the 13 5/8-inch casing with a
cutting torch, a flash fire occurred due to gas emanating from the oil-based mud. It
quickly went out on its own. They were cutting the casing to install the wellhead.
| Date: |
14-Nov-1999 |
Operator: |
CXY Energy Offshore, Inc. |
| Investigation: |
Complete |
Activity: |
Development/Production |
| Lease: |
G00985 |
Event(s): |
Fire |
| Area: |
Eugene Island |
Operation: |
Production |
| Block: |
259 |
Cause: |
Equipment Failure |
| Rig/Platform: |
B |
Water Depth: |
170 feet |
Remarks: Two Halliburton wireline operators were to perform
maintenance service on a Halliburton wireline unit. The wireline unit was approximately 20
feet from the compressor unit skid. The operators heard a loud uncontrolled release of
natural gas blowing from the compressor unit. They observed the uncontrolled gas release
for approximately 1 minute, assuming the compressor unit would shut down. The released gas
accumulation apparently came into contact with the hot surface of the turbocharger
assembly and engine exhaust system (estimated temperature 900° F), resulting in ignition.
An operator reported the fire to CXY Energy personnel stationed on Platform A and
activated the platform ESD. The operators fought the fire with a 150-lb. wheeled unit and
6 30-lb. handheld extinguishers. Three employees arrived on the platform to help
extinguish the fire and isolate the compressor by closing the upstream manual block
valves. The volume of natural gas remaining in the compressor 3rd stage
scrubber continued to escape though a parted 1-inch nipple. The M/V Jansen G arrived and
began spraying water on the compressor unit with its onboard fire monitor, cooling the hot
surfaces of the gas compressor unit, allowing the platform personnel to completely
extinguish the fire. The fire was extinguished and re-ignited 6 times, diminishing in
magnitude each time. There was major damage to the platform compressor unit.
| Date: |
14-Nov-1999 |
Operator: |
BP Exploration & Oil, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G11081 |
Event(s): |
Fire |
| Area: |
Green Canyon |
Operation: |
Production |
| Block: |
645 |
Cause: |
Equipment Failure |
| Rig/Platform: |
Ocean America |
Water Depth: |
4,352 feet |
Remarks: Sealed bearings in the drill water pump #1 heated
to the point of smoking while in service. A small fire occurred when the pump was shut
down.
| Date: |
15-Nov-1999 |
Operator: |
BP Amoco Corporation |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G05825 |
Event(s): |
Fire |
| Area: |
Mississippi Canyon |
Operation: |
Production |
| Block: |
109 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A/H&P 91 |
Water Depth: |
1,035 feet |
Remarks: The insulation on the Amberbrol circulation system
caught fire. The fire was put out with an extinguisher. There were minimal damages.
| Date: |
16-Nov-1999 |
Operator: |
CXY Energy, Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
00138 |
Event(s): |
Fire/Injury (1) |
| Area: |
West Delta |
Operation: |
Production |
| Block: |
45 |
Cause: |
Human Error |
| Rig/Platform: |
A |
Water Depth: |
49 feet |
Remarks: During the welding of a flange on the inlet piping
of a production vessel, a flash fire occurred. One welder was burned.
| Date: |
20-Nov-1999 |
Operator: |
Texaco Exploration and Production |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G06987 |
Event(s): |
Fire |
| Area: |
Green Canyon |
Operation: |
Production |
| Block: |
6 |
Cause: |
Equipment Failure |
| Rig/Platform: |
A |
Water Depth: |
620 feet |
Remarks: A 3/8-inch steel line filled with coolant cracked
and allowed fluid to spill onto the compressor feets turbo-charger. It produced a small
fire with no damage. The compressor then went down. While the operator was attempting to
restart the compressor, he noticed the small fire and immediately extinguished it.
| Date: |
22-Nov-1999 |
Operator: |
AEDC (U.S.A.), Inc. |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G06957 |
Event(s): |
Fire |
| Area: |
Mississippi Canyon |
Operation: |
Welding |
| Block: |
486 |
Cause: |
Human Error |
| Rig/Platform: |
A |
Water Depth: |
582 feet |
Remarks: While welding on the top deck, a spark from a
welding rod fell down into the drip pan for the glycol reboiler and ignited a small amount
of condensate in the pan. The fire was immediately extinguished. There was no damage to
the platform.
| Date: |
27-Nov-1999 |
Operator: |
Mobil Oil Corporation |
| Investigation: |
None |
Activity: |
Development |
| Lease: |
G03417 |
Event(s): |
Fire |
| Area: |
Main Pass |
Operation: |
Production |
| Block: |
72 |
Cause: |
Equipment Failure |
| Rig/Platform: |
B |
Water Depth: |
120 feet |
Remarks: Steam was observed near the turbo charger exhaust.
An ambitrol line was spraying fluid from a loose chemical line onto the exhaust, causing a
small fire on the compressor turbo charger exhaust. The fire was extinguished immediately
with minimal damage.
| Date: |
02-Dec-1999 |
Operator: |
Amerada Hess Corporation |
| Investigation: |
Complete |
Activity: |
Exploration |
| Lease: |
G21175 |
Event(s): |
Fire |
| Area: |
Mississippi Canyon |
Operation: |
Drilling |
| Block: |
553 |
Cause: |
Equipment Failure/Human Error |
| Rig/Platform: |
Diamond Ocean Valiant |
Water Depth: |
4,513 feet |
Remarks: A welder was replacing bad grating on the catwalk
leading to the master dump valves under the main deck. Cutting and welding operations were
going on at the same time. The rig crew started transferring "ECO-MUL 300" from
internal tanks in the hull to the active mud pits. The rig crew was having trouble priming
the base oil transfer pump; when the pump did catch prime, it blew the fluid out of a
loose flange on the main deck level. The fluid spilled down the side of the rig structure
and onto the catwalk where the welder was working, igniting. A crane operator working in
the area immediately spotted the fire. The base oil transfer pump was shut down and the
oxygen and acetylene bottles were turned off. The well was shut in and fire teams
extinguished the fire in approximately ten minutes.
| Date: |
15-Dec-1999 |
Operator: |
Vastar Resources, Inc. |
| Investigation: |
Complete |
Activity: |
Development |
| Lease: |
G03998 |
Event(s): |
Fire |
| Area: |
Ship Shoal |
Operation: |
Production |
| Block: |
182 |
Cause: |
Human Error |
| Rig/Platform: |
C |
Water Depth: |
70 feet |
Remarks: The platform was in the process of starting up
after a two-day shut in for maintenance. The heat media surge tank had a high level alarm
when the heat media system came back in service. They attempted to drain the Chem Therm
from the heat media surge tank into a drum, but the surge tank level was still too high.
Another attempt to drain the surge tank resulted in spilling the fluid onto the insulated
generator muffler located on the deck below; the fluid found its way to the hot surface
and ignited. At the same time, the drum bubbled Chem Therm onto the surge tank, which also
ignited. The automatic shut in of the platform was initiated via a TSE. The fire was
extinguished with handheld fire units.
Last Updated:
09/17/10,
05:07 PM
|