|
Gulf of
Mexico Region
Spills ≥ 50
Barrels (2,100 gallons) – 2009
January to March,
2009 – W & T Offshore, Inc.
|
Pollution: |
54.3 bbl |
Crude
Oil/ Condensate: |
54.3 bbl
Crude Oil |
|
Refined Petroleum: |
None |
Synthetic Oil Fluids*: |
None |
|
Chemicals: |
None |
Event: |
Pollution |
|
MMS Investigation Report: |
Accident Incident Reports Only |
Activity: |
Decommissioning/Salvage |
|
Lease: |
G05525 |
Operation: |
Submerged Platform |
|
Area: |
Eugene Island |
Causes: |
Hurricane Ike |
|
Block: |
371 |
Distance to Shore: |
93 Miles |
|
Platform: |
B |
Water Depth: |
415 Feet |
Remarks: The
Eugene Island 371 B 4-pile fixed platform with skirts,
installed in Federal waters in 1987, was destroyed by Hurricane
Ike in September 2008. Approximately 54.3 bbl seeped from the
structure between January 1 and March 31, 2008.
NRC Report: None
April 19, 2009 – LLOG
Offshore, Inc.
|
Pollution: |
200 bbl |
Crude
Oil/ Condensate: |
None |
|
Refined Petroleum: |
None |
Synthetic Oil Fluids*: |
None |
|
Chemicals: |
200 bbl Calcium Bromide |
Event: |
Loss of Well Control, Pollution |
|
MMS Investigation Report: |
2010 Form Completed 8-December-2009 |
Activity: |
Development/Production |
|
Lease: |
G08483 |
Operation: |
Completion |
|
Area: |
Mississippi Canyon |
Causes: |
Equipment Failure |
|
Block: |
72 |
Distance to Shore: |
34 Miles |
|
Platform: |
Noble Lorris Bouzigard |
Water Depth: |
2,013 Feet |
Remarks: Loss
of Well Control. Operating from the semisubmersible drilling
rig Noble Lorris Bouzigard, after perforating the subject well
during the initial completion operation, the hole lost 14.4 ppg
calcium bromide completion fluid. Gas in riser and 200 bbl of
calcium bromide completion fluid was discharged through the
diverter. All non-essential personnel were mustered at the stern
life boat stations donning life jackets as the general
evacuation alarm sounded, but no actual rig evacuation took
place. No clear and specific cause could be identified for the
gas bubble to have traveled into the riser prior to the first
surface observed trip tank gain and closure of the BOP Upper
Annular subsequent to intentionally unseating the Champ IV
Packer. The reverse shock wave created by the perforating guns
may have momentarily opened a valve allowing for a gas bubble
flow path to the annulus.
Accident Investigation Report:
Form 2010 19-April-2009 MC 72
NRC Report: 903185
May 3, 2009 – Shell
Offshore Inc.
|
Pollution: |
70.0 bbl |
Crude
Oil/ Condensate: |
None |
|
Refined Petroleum: |
None |
Synthetic Oil Fluids*: |
None |
|
Chemicals: |
70.0 bbl Methanol |
Event: |
Pollution |
|
MMS Investigation Report: |
Accident Incident Report Only |
Activity: |
Development/Production |
|
Lease: |
G08241 |
Operation: |
Production |
|
Area: |
Garden Banks |
Causes: |
Equipment Failure |
|
Block: |
426 |
Distance to Shore: |
168 miles |
|
Platform: |
A - Auger |
Water Depth: |
2,860 Feet |
Remarks: While
the operator on the Garden Banks A-Auger tension leg platform
(installed in 1994) was attempting to equalize pressure across a
subsea safety valve (SCSSV) on a well prior to opening it. When
58 bbl of methanol were pumped into a methanol line feeding a
group of three wells, the methanol flowed either into one of the
other two wells, via a malfunctioning valve, or was released to
the environment through a leak. Because this leak was at a
subsea location with a 2860 foot water depth and the tubing
interconnections are complex, the diagnostic process is
complicated. In the process of identifying the leak, an
additional 12 bbl of methanol was pumped through the tubing
during tests, for a total release of 70 bbl of methanol prior to
securing the leak.
NRC Report: 904605
and
904792
May 28, 2009 – Devon
Energy Production Company, Inc.
|
Pollution: |
102.7 bbl |
Crude
Oil/ Condensate: |
None |
|
Refined Petroleum: |
None |
Synthetic Oil Fluids*: |
102.7 bbl Synthetic Base
Fluids in 223.3 bbl of 46% Rheliant SBM |
|
Chemicals: |
None |
Event: |
Pollution |
|
MMS Investigation Report: |
2010 Form Completed
27-July-2009 |
Activity: |
Exploration |
|
Lease: |
G19545 |
Operation: |
Drilling |
|
Area: |
Keathley Canyon |
Causes: |
Equipment Failure & Human Error |
|
Block: |
291 |
Distance to Shore: |
200 miles |
|
Rig: |
Seadrill West Sirius |
Water Depth: |
5,851 Feet |
Remarks: Devon
Energy reported 223.3 bbl of 46% Rheliant 46% synthetic based
mud (SBM) was unintentionally discharged from the Seadrill West
Sirius semisubmersible drilling rig (built in 2008) into the
Gulf of Mexico. This discharge was a result of an incorrect
valve lineup on the hydraulic supply to the Diverter Control
Unit. It is estimated that the lost SBM contained approximately
102.7 barrels of synthetic base fluids. In addition, prior to
discovering the incorrect valve line-up, returns were lost
during cementing operations with no evidence that the trip tank
was not being properly monitored. The investigation determined
that an improper seal of the telescopic slip joint resulted from
the lack of hydraulic supply pressure causing the loss of SBM. A
hydraulic supply block valve was inadvertently left closed
following recent maintenance operations, leading to inadequate
pressure to seal the slip joint.
Accident Investigation Report:
Form 2010
28-May-2009 KC291
NOAA Incident News:
8029
NRC Report:
906859
July 25, 2009 – Shell
Pipeline Company
|
Pollution: |
1,500 bbl |
Crude
Oil/ Condensate: |
1,500 bbl
Crude Oil |
|
Refined Petroleum: |
None |
Synthetic Oil Fluids*: |
None |
|
Chemicals: |
None |
Event: |
Pollution |
|
MMS Investigation Report: |
U.S. DOT Report 17-Aug-2009 |
Activity: |
Development/Production |
|
Lease: |
G23900 |
Operation: |
Pipeline, Production |
|
Area: |
Ship Shoal |
Causes: |
External forces |
|
Block: |
142 |
Distance to Shore: |
33 miles |
|
Pipeline Segment: |
# 4006 |
Water Depth: |
50 Feet |
Remarks: At 6:00
p.m. on Saturday, July 25, 2009, the Shell Pipeline Company
shut-in the Eugene Island Pipeline System (EIPS) due to the loss
of pressure. The DOT-regulated 20" oil pipeline segment #4006
(originating in South Marsh Block 128 and terminating in South
Timbalier Block 11) installed in Federal waters in 1996, had
developed a leak in Ship Shoal Block 142. The Marine Spill
Response Corporation (MSRC) responded to the spill. A total of
220 gallons of Corexit 9527 dispersants were applied on Monday
by the MSRC's
King
Air aircraft. Two of MSRC's
responder class vessels were dispatched, the
Louisiana
Responder began skimming on Monday
morning, and the
Gulf
Responder was on site Tuesday.
Approximately 1,500 barrels were released of which 276 barrels
were recovered.
The spill was caused by a
longitudinal crack on the EIPS at the crossing point with a
third party pipeline (Williams pipeline). The force and energy
of multiple storms (i.e. Hurricanes Rita, Gustav, Ike, etc.)
scoured the seabed and washed out the original pipeline
separation at the crossing and damaged the concrete coating.
Mechanical damage observed at the EIPS failure point included
multiple small, very shallow surface gouges in a concentrated
area, along with some deformation of the pipeline in the same
area. The gouges and deformation were probably caused by severe
abrasion and gouging that resulted from repeated contact with
the Williams pipeline after the original pipeline separation
failed. The abrasion and contact subsequently promoted the
expansion of the micro-fractures in the pipe wall until normal
operational pressure cycling and fluctuations caused pipe
failure.
In an "Accident Report -
Hazardous Liquid, Pipeline Systems" submission to the U.S.
Department of Transportation, Shell Pipeline Co. estimated total
costs of $10,723,000: $20,000 Public/private property damage,
$3,500,000 Cost of emergency response phase, $103,000 Value of
product lost, and $7,100,000 Repair costs.
NRC Report:
912739
NOAA Incident News:
8061
October 25, 2009
– Shell Offshore Inc.
|
Pollution: |
314 bbl |
Crude
Oil/ Condensate: |
None |
|
Refined Petroleum: |
None |
Synthetic Oil Fluids*: |
314 bbl
Accolade Synthetic Base |
|
Chemicals: |
None |
Event: |
Pollution |
|
MMS Investigation Report: |
2010 Form
Completed
2-April-2010 |
Activity: |
Development/Production |
|
Lease: |
G05868 |
Operation: |
Drilling |
|
Area: |
Mississippi Canyon |
Causes: |
Human
Error |
|
Block: |
765 |
Distance to Shore: |
79 Miles |
|
Rig: |
Noble Jim
Thompson |
Water Depth: |
3,544
Feet |
Remarks: On 25
October 2009, at approximately 1830 hours, 314 bbls of Accolade
Base Fluid (Accolade), a synthetic base mud additive, was
discharged overboard. A pontoon hand inadvertently pumped out
the MPP-02 tank containing the Accolade when he assumed it was
seawater. The pontoon hand discharged the contents into Gulf
waters without reading the rig logs or verifying the contents of
the tank. The Pontoon hand was notified five hours later that
the Accolade and not seawater was in tank MPP-02. At the time of
the incident, the rig was in the process of pulling anchors to
move off location. The pontoon hand did not read the rig log of
19 October 2009 which states that the fluid was transferred to
tank MPP-02, but instead assumed that seawater was in the tank.
No testing of the tank(s) fluids were performed prior to the
discharge operation. No signs were installed on the tank(s) to
indicate their contents.
Accident Investigation Report:
Form 2010 25-October-2009 MC765
NRC Report: 921720
November 10, 2009 –
BP Exploration & Production
|
Pollution: |
60 bbl |
Crude
Oil/ Condensate: |
None |
|
Refined Petroleum: |
None |
Synthetic Oil Fluids*: |
60 bbl
synthetic base oil in 97 bbl of 62% SBM |
|
Chemicals: |
None |
Event: |
Pollution |
|
MMS Investigation Report: |
2010 Form
Completed
10-February-2010 |
Activity: |
Development/Production |
|
Lease: |
G15607 |
Operation: |
Drilling |
|
Area: |
Green
Canyon |
Causes: |
Equipment
Failure |
|
Block: |
743 |
Distance to Shore: |
122 Miles |
|
Rig: |
GSF
Development Driller II |
Water Depth: |
6,824
Feet |
Remarks: The GSF
Development Driller II, a semi-submersible drilling rig, was in
the process of flushing the kill, boost, and choke lines. While
flushing the choke line with synthetic based 11.7 pound per
gallon mud, operating personnel realized the choke line had been
detached from the gooseneck on the slip joint and was hanging in
the water suspended from the connection. A total of 97 bbl of
62% synthetic based mud (SBM) was released through the choke
line into the water. It is estimated that the lost SBM contained
approximately 60 bbl of synthetic base fluids.
Accident Investigation Report:
Form 2010 10-November-2009 GC 743
NRC Report:
923144
December 3, 2009
– LLOG Exploration Offshore Inc.
|
Pollution: |
230 bbl |
Crude
Oil/ Condensate: |
None |
|
Refined Petroleum: |
None |
Synthetic Oil Fluids*: |
None |
|
Chemicals: |
230 bbl
of Zinc Bromide |
Event: |
Pollution |
|
MMS Investigation Report: |
2010 Form
Completed
8-January-2010 |
Activity: |
Exploration |
|
Lease: |
G31694 |
Operation: |
Completion |
|
Area: |
Green
Canyon |
Causes: |
Human
Error |
|
Block: |
97 |
Distance to Shore: |
93 Miles |
| Rig: |
Noble
Lorris Bouzigard |
Water Depth: |
650 Feet |
Remarks: During a
fracturing job, the Noble Lorris Bouzigard, a semi-submersible
drilling rig, discharged 230 barrels of 15.7 pound per gallon
Zinc Bromide completion fluid overboard. During fluid
circulation, an incorrectly positioned valve on the gumbo box,
at the end of the mud line, caused the Zinc Bromide to flow in
the master drain line and ultimately overboard.
Accident Investigation Report:
Form2010 3-December-2009 GC 097
NRC Report:
925218
December 19, 2009
– BP Exploration & Production Inc.
|
Pollution: |
50
bbl |
Crude
Oil/ Condensate: |
50
bbl Crude Oil |
|
Refined Petroleum: |
None |
Synthetic Oil Fluids*: |
None |
|
Chemicals: |
None |
Event: |
Pollution |
|
MMS Investigation Report: |
2010 Form Completed
22-February-2010 |
Activity: |
Development/Production |
|
Lease: |
G15610 |
Operation: |
Production |
|
Area: |
Green Canyon |
Causes: |
Equipment Failure |
|
Block: |
782 |
Distance to Shore: |
134 Miles |
|
Platform/Rig: |
A-Mad Dog |
Water Depth: |
4,420 Feet |
Remarks:
On 19 December 2009, BP Exploration
and Production Inc's Mad Dog spar had a pollution event
resulting in approximately 50 barrels of oil going into the
water of the moon pool center well. An operator observed crude
oil on the surface of the center well, as a result, all hot work
was ceased and fire crews were put on watch. The oil was
reported as being dark black and having a strong smell. BP
removed all oil from the center well caisson and began regular
monitoring of the center well. An investigation determined a
faulty check valve was the cause of oil entering the caisson.
The valve was repaired and double isolated with manual block
valves. The check valve remains isolated until the piping design
is corrected to prevent another occurrence.
Accident
Investigation Report:
Form 2010 19-December-2009 GC 782
NRC Report:
No NRC Report
December 24, 2009
– Anadarko Petroleum Company
|
Pollution: |
124.5 bbl |
Crude
Oil/ Condensate: |
None |
|
Refined Petroleum: |
None |
Synthetic Oil Fluids*: |
124.5 bbl
synthetic base oil in 196 bbl of 63.5% SBM |
|
Chemicals: |
None |
Event: |
Pollution |
|
MMS Investigation Report: |
Accident Incident Report Only |
Activity: |
Development/Production |
|
Lease: |
G21826 |
Operation: |
Drilling |
|
Area: |
Atwater Valley |
Causes: |
Equipment
Failure |
|
Block: |
37 |
Distance to Shore: |
196 Miles |
|
Rig: |
Transocean Discoverer Spirit
|
Water Depth: |
8,232
Feet |
Remarks: Personnel
on the T.O. Discoverer Spirit drillship discovered. A leak
occurred in the kill line connection between two joints at a
true vertical depth of 7,449 feet. Initially 48 bbl of 11.2 ppg
synthetic based mud (SBM) was lost due to the leak. An
additional 148 bbl SBM, the capacity of the kill line, was lost
due to the leak. A total of 196 bbl of 63.5% SBM was released.
It is estimated that the lost SBM contained approximately 124.5
bbl of synthetic base fluids.
NRC Report: 927042
December 30, 2009
– Murphy Exploration & Production Company
|
Pollution: |
62.0 bbl Preliminary |
Crude
Oil/ Condensate: |
62.0 bbl |
|
Refined Petroleum: |
None |
Synthetic Oil Fluids*: |
None |
|
Chemicals: |
None |
Event: |
Loss of
Well Control, Pollution |
|
MMS Investigation Report: |
Ongoing Panel Investigation |
Activity: |
Exploration |
|
Lease: |
G27306 |
Operation: |
Plugged &
Abandoned |
|
Area: |
Mississippi Canyon |
Causes: |
Equipment
Failure |
|
Block: |
736/737 |
Distance to Shore: |
73 Miles |
|
Well: |
No. 1 |
Water Depth: |
6,050
Feet |
Remarks: Small
leak discovered at plugged and abandoned wellhead. Well was
repaired in January 2010. Information preliminary pending
completion of the Panel Investigation.
NRC Report:
927630
One Barrel (bbl) Equals 42 U.S.
Gallons (gal)
|
U.S. Coast Guard Spill Size
Categories |
MINOR |
MEDIUM |
MAJOR |
|
Less than 238 barrels (Less than
10,000 gallons) |
238 to 2,380 barrels (10,000 to
99,999 gallons) |
2,381 barrels and more (100,000
gallons and more) |
| Size
Categories are for coastal and offshore waters and
are based solely on spill volume. |
Synthetic Oil Fluids*:
In deepwater drilling, synthetic-based
muds (SBM’s) are preferred over petroleum oil-based muds (OBM’s)
due to the SBM's superior performance properties. The synthetic
oils used in SBM’s are relatively non-toxic to the marine
environment and have the potential to biodegrade.
60%**:
Indicates that for a
synthetic-based mud release, the exact percentage of volume of
synthetic base oil to total volume of mud released was not
available and 60% was used as a reasonable approximation.
75%***:
Indicates that for an oil-based
mud release, the exact percentage of volume of base oil to total
volume of mud released was not available and 75% was used as a
reasonable approximation. Diesel is assumed to be the base oil
in OBM unless otherwise specified. |